Ian Pearson reports a fine, mild, slightly overcast day at Grosmont with Bill Dobson, Nigel Bill, Jon Bradley, Nigel Hall and Ian himself. With the stove lit and kettle on it was cups of tea ☕️ all round and a catch-up with Barney at the MPD. The J27 had been steam tested on Tuesday and it was found to have steam leaks from the front valve covers and the whistle.
So those were the jobs for the day. Bill worked on the J27 whistle all day which he stripped down, cleaned, sealed and re-fitted, while Nigel B and Ian worked on the valve covers with Jon assisting later after he completed some lagging work in the Q6 cab. The J27 oil pipes and cylinder cock front drain pipes were removed. This was not easy as the locomotive wasn’t on a pit and there was no chance of getting on one as 5428 was on steam test for the boiler inspector on the top pit and No 5 Road pit was full with the B1 and 76079. So work had to be done on the ground outside No 4 Road sat on cardboard with cushions on top. Meanwhile, Nigel H removed the Q6 cab numbers and spent the day sanding the cab sides and sand boxes.
Lunch was had around the stove and Ian warmed his steak pie on the stove hot plate - please note Trevor! After lunch the valve covers were eventually removed, the faces cleaned, and a ptfe seal put around each cover - the same material as was put round the Q6 cylinder cover. Then the covers were re-fitted and secured, and the oil pipes and drain cock pipes re-fitted. Hopefully it will now be OK for its scheduled workings during the Big Engine service over the next week. However, the right hand side hand rail has come out of its socket again and will have to have another socket welded onto the existing socket to secure it.
Some of the shed staff were working at Newbridge getting Repton and City of Wells (replacing Union of South Africa for the Big Engine service over the next week, as No 9 is still undergoing repair) ready for moving to Grosmont tomorrow.