North Eastern Locomotive Preservation Group

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Home Locomotives Q6 63395 (NER T2 2238) Q6 Blog 23rd to 28th October 2021 - Q6 Test Runs

23rd to 28th October 2021 - Q6 Test Runs

The end of the line! Bill Dobson takes a bow after the Q6 hauls it's first train since overhaul - Jonathan Bradley

The Q6 is finally back in revenue earning service, so many thanks to Bill and Ian Pearson in particular, but also to everyone else who has been involved over the past two years, for all their hard work in overcoming frustrating setbacks and problems, culminating in the successful arrival at Pickering on the Thursday of 63395 with the 14.30 departure from Grosmont.

During the final assembly of the locomotive one of the cylinder cover studs was not as tight as it should have been on the casting. On steaming, hairline cracks were noticed around an old metal stitching repair. A new repair was effected, and a stepped stud fitted in the offending location. The mating surface was not flat, so it was arranged that an on-site machining company should skim the front face of the cylinder casting. This also cured a long standing issue whereby the cylinder liner was not flush with the casting.

Saturday 23rd October 2021

A fine day at Grosmont and, along with Bill, Ed Bolam and Ian, were two engineers from Team Industrial Services who had come to skim the righthand cylinder face. This job was completed by mid afternoon, but it was a bit late to start refitting the studs and cover, so it was agreed to come in on Monday to fit the cover.

The Team Industrial Services jig facing the RHS cylinder - Ed Bolam

A movie by Ed Bolam showing the machine in action can be seen here.

The RHS cylinder after facing - Ed Bolam

 

Monday 25th October

Monday dawned a fine day at Grosmont, with a couple of heavy showers at lunchtime for Bill Dobson, Ian MacCall and Ian Pearson to dodge. The first job was to fit the 20 studs back into the cylinder face, but also to remove the lubricator drive and big end brasses from con rod in readiness for a bump test later.

After the studs had been fitted, the cover was put in position on the lifting table and pushed onto the studs with some of the nuts applied. It was then found that it would not fit snugly, so the cover was removed. The stepped stud that was fitted last week looked slightly out of line with the others. As a result, the hole in the cover that it fits on was slightly enlarged with the die grinder and the cover refitted. But it still would not fit in against the cylinder face. So, the cover was removed again, and fitting was tried without the copper ring. No luck! It still would not fit, so the cover was removed once more. Bill ground round the tapered area of the inside of the cover that fits into the cylinder and then another fitting was tried. This time it was a lot better but still not good enough. After consulting Sean Bowler, he suggested putting the cover on the vertical borer to skim off a few thou. As it was 6pm, this was decided to be a job for Tuesday morning, the cover was taken off again, put on the lifting table, and taken to the machine shop ready for machining the next day.

Tuesday 26th October

63395 right hand cylinder cover being skimmed on the vertical borer in Grosmont MPD by Sean Bowler on 26 October 2021 - Ian Pearson

Today's volunteers were Bill Dobson, Steve Hyman and Ian Pearson, and the first job was to take a slight amount off the copper ring which was slightly overlapping the entrance of the cylinder bore on the left side. This was done with a flapper wheel by Sean Bowler. Then, down in the machine shop, the cylinder cover was set up on the vertical borer and skimmed, taking off about 20 thou (see photo). It was then refitted successfully and tightened up with Bill using a torque wrench to the required amount. After the cover was fitted, a bump test was carried out successfully and the big end brasses refitted and secured with some help and assistance from Chris Cubitt. The warming fire, which was set on Monday, was lit during the afternoon. Other work done was making and fitting of a plywood cover over the driver’s side sand box.

Wednesday 27th October 2021 - First run to Goathland

Bill and Ed Bolam on duty. The Q6 was in steam, and with Charlie Wood driving and Andrew Jeffery firing, the Q6 did a couple of successful running in trips to Goathland (see photos).

All looks fit to go. Andrew Jeffery and Bill Dobson complete preparation - Ed Bolam

Backing down to the Station - Ed Bolam

63395 being checked at Grosmont by Bill Dobson and Charlie Wood on 27 October 2021 before its first running in trip to Goathland following overhaul - Andrew Jeffery

With a beaming Andrew Jeffery in the fireman's seat, the Q6 passes the shed on the first run to Goathland - Ed Bolam

Thursday 27th October 2021 - Another run to Goathland

Thursday was a fine windy day with the Q6 in steam again, with Bill in attendance and driver Robson Hewitson and fireman Graham Hartley. It did two more running in trips to Goathland light engine with no problems, and then worked the five coach 14.30 return to Pickering from Grosmont (see photo) and was relieved on its return to Grosmont by the Class 20, Sir John Betjeman, to take the train on to Whitby. The engine performed well, with only the lefthand big end slightly warmer than the righthand one. The lefthand big end is on the list to be adjusted.

With cylinder cosmetic covers now fitted, departing at 12.05 light engin to Goathland - NYMR Grosmont webcam

Passing MPD Shed - Nigel Bill

Crossing over arriving 12.15 at Goathland - NYMR Goathland webcam

The first loaded train

Resting in the occasional bit of sun at Grosmont - NYMR Grosmont webcam

Bill Dobson climbs aboard the 14.55 - NYMR Grosmont webcam

Passing the J27 outside Deviation Shed - Nigel Bill

Arriving 15.11 at Goathland - NYMR Goathland webcam

Arriving at Pickering - Jonathan Bradley

After running round, the Q6 comes onto the train for the return to Grosmint - Jonathan Bradley

The Q6 is now back in service.

Many thanks to all those, both NELPG and NYMR, who have worked so hard over the last two years to make this possible.